
Connected the fuel lines and pressure tested the system. Found out that there is a small leak in fuel rail welding. Have to weld that and figure out a bit of wiring and then it would be the start up time. So no start up this week

Yes, it is a completely stock 2.3 bottom end. In dyno it pushed 520Whp. We did drop timig 3 degrees after the tuning, so with that it had ~480whp in use. I think that when I get this new stock engine put together I am going to drive with 1.4 bar boost. With boost controller I have 1.8bar on peak torque and 1.6bar on peak hp. Maybe with 1.4bar boost it won´t break this summer anymore.Narux skrev:Are you running stock conrods? How much Hp does the engine make?
I do have one complete 2.0 engine, but it would require new dyno session to get it working properly and I don´t have time for it. Also I have a set of 2.0 T7 Wössner pistons and a set of forged 153mm pistons, but they are not going into this setup.MickeK skrev:Build with 2.0 piston and rods or change to t7 piston and 153mm rods.
I never have this problem when I have this setup
Well it isn´t going back this week. Maybe next week or week after that.keme skrev:I´ll get the cylinder head back from the machinist on Monday so the engine should be going back in next week.